GRUPO PRIMEX  

THE COMPANY

Grupo Primex began its operations in 1968 and has occupied an international market position since 1983.  It is a part of AXA-Yasaki, a large Mexican industrial conglomerate currently made up of 18 companies, with a total of 27 production plants and distribution centers operating in Mexico, the United States, Argentina and Brazil.

Grupo Primex currently has four process plants for polyvinyl chloride (PVC) resins and compounds, phthalic anhydride, dioctyl phthalate plastifiers (DOP) and trioctyl trimethylate (TOTM), with an annual  production of 450,000 tons.  Its petrochemical complex is located at Altamira in the southern part of the State of Tamaulipas, and it is considered to be the largest company of its kind in Mexico.  It is the domestic market leader and exports 40% of its annual production to the United States, England, Germany, Italy, Japan, South Africa and Australia.

The vision Grupo Primex has is:

  • To be a generator of wealth with worldwide leadership in satisfying its customers;
  • To be the lowest price producer and to maintain an international focus in managing its business; and
  • To be a company that is committed to its statements and principles.

THE PROJECT

Grupo Primex found out that its DOP plastifier was picking up an odor during the manufacturing process.  Since its main use is in food packing and specifically in the manufacture of plastic cap liners, this is an undesirable feature in DOP because it contaminates the packed food.  For this reason, a project was begun for obtaining a food grade DOP, which means that it must be odorless and flavorless.  The DOP also needed to have certain physical features such as a percentage of humidity of 0.05 or less, and less than 150 ppm of alcohol.

DESCRIPTION OF THE PROCESS

The manufacturing process for DOP plastifier consists of the following stages:

1) Raw Material Loading. This consists of loading the raw materials (phthalic anhydride and alcohol) into the reactor.

2) Heating up to Catalyst Loading Temperature.  Here, heat is transferred to the reaction through a coil and jacket in the reactor to enable the catalyst to work.

3) Reaction. This is the chemical reaction between the phthalic anhydride, alcohol and catalyst for making the plastifier.

4) Cooling of Plastifier.  Heat is removed from the reaction product by running steam through the reactor coil.

5) Neutralization.  A chemical base (pH over 7) is added to eliminate final acidity in the product.

6) Unloading Reactor.  This consists of sending the product from the reactor to a treatment tank (tank Blow Down).

7) Alcohol Recovery. Vacuum pressure is applied in the tank itself, which causes the temperature to rise to 176 ºC.  This causes the alcohol to evaporate, which is exhausted through a pipe to a storage tank for use in a prior stage.

8) Distilling.  This stage consists of running steam through the plastifier to pull the remaining alcohol out of the product.  This is accomplished in a two hour period and uses approximately 4,000 kg/hr of steam at maximum vacuum.

9) Cooling.  This is accomplished by condensing in which the plastifier is cooled down to 115 °C, then demineralized water at low temperature is run through the coil.

10) Washing.  This is accomplished by running two tons of demineralized water through the plastifier for removing impurities from it.

10) Drying.  Drying is done by heating the product to 145 °C at maximum vacuum to remove moisture from it.  It should be emphasized that according to staff from the PRIMEX production department, this heating encourages oxidation in the plastifier, thus causing an odor to be generated in the resulting DOP.

11) Tank Unloading.  Product is removed by tank Blow Down at 145 °C and it is sent to a treatment tank where additives are put in and it then goes to filtering.

12) Filtering.  The product is run through a porous medium to remove solid residue.  This system consisted of filtering in an uncovered tank (in contact with the atmosphere), either through a valve or by venting.

DOP Manufacturing Flowchart
 Finished product  

ECOEFFICIENCY STRATEGY APPLIED

After studies were made by the company, process changes were put in place that brought about a significant decrease in carbon dioxide (CO2) emissions to the atmosphere, which shows the environmental tack taken by this project developed by the company.  It is important to mention that there was no need for making any initial investment, because the only thing that was done was to make process changes that did not cost anything.  Process stages were changed to be as follows:

  • Recovery:  Recovery temperature was changed to 178 °C and vacuum pressure was increased.
  • Distilling:  This stage was not changed at all, and it is still accomplished in two hours by using approximately 4,000 kg/hr of steam at maximum vacuum..
  • Cooling:  Condensing through the reactor coil is still being used, but it is now being cooled to 125 °C.  Washing is performed by using the same amount of demineralized water.
  • Drying:  Heating is no longer used for drying. Cold nitrogen is now being used (approximately 87 cubic meters at 105 °C, because that is its temperature after washing) to carry off moisture and discourage product oxidation as was happening before, and also by using maximum vacuum at this stage.
  • Unloading:  Unloading is now done at 95 °C, which is the temperature at which the product comes out after drying, because the nitrogen also cools the product in addition to drying it.
  • Filtering:  There is currently a hatch sealing the tank and leading to a pipeline to keep the system inert, and in this way contact between the product and oxygen in the environment is avoided and thus, oxidation of the product.

With these changes, a significant improvement in CO2 emissions was achieved as a result of making steam in the process by using a boiler with 80% efficiency, which brought about a natural gas (CH4) use decrease of 569,400 cubic meters.  This also resulted in avoiding the emission of an approximately 55,235 cubic meters of CO2 into the atmosphere, which is the main cause of global heating on the planet.

Daily nitrogen consumption increased from 740 a 800 cubic meters, but unlike natural gas, nitrogen use in drying does not have any adverse impact on the environment.

FINANCIAL BENEFITS

The financial benefit is mainly from the savings represented by decreased steam generation and by replacing this with the use of nitrogen in the drying stage for the plastifier, and the following cash flow benefit has been achieved on an annual basis:

Raw Material

Cost (US $/year)

Saved (US$/year)

Methane

44,800

Nitrogen

8,200

 Total Savings

36,600 US$/year

CONCLUSIONS

Results achieved with this project were better than expected.  The original aim was to obtain odorless DOP.  A study was done with this goal in mind, and the DOP that was desired was obtained with zero investment.  Costs were also substantially decreased, thus providing a significant annual cost savings.  This ecoefficiency program was also positive in its results because in addition, this savings in methane gas brought about a substantial decrease in carbon dioxide emissions into the atmosphere.

GLOSSARY

Plastic Cap Liners:  Used as lining inside caps for bottles, jars, etc.
Coil :  Coiled tubing installed around the center paddle shaft of the tank and reactor but not touching it, used for running fluids through it to either cool or heat the product in the container through a convection process.
Blow Down tank:  Multiple treatment tank where the finished product acquires its final characteristics.

CONTACT

Ing. Martín Conde Carreño
Safely & Environmental Superintendent
km 4.5 Autopista Altamira - Tampico
Nuevo Puerto Industrial
Altamira, Tamaulipas, Mexico
Tel. (52 1) 229 0115
Fax. (52 1) 260 0066
e-mail: mconde@gpoprimex.com